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After learning how the car performs bone stock, we set about adding a few "improvements." The first modifications were a Buschur Racing 3" exhaust and Buschur Racing intake. See the first few dyno charts below.
On 6/11/03, we installed a S-AFC and picked up a ton of power -- 30 hp to the wheels! We noticed some odd behavior where the stock boost controller would reduce boost momentarily around 4500 rpms. A Hallman mechanical boost controller fixed that, and added a few more horsepower.
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 | Dyno plot: Stock and with intake/exhaust Stock hp 221.3, torque 240.9

|  |  | Dyno plot: Installed Buschur Racing intake Max hp 229.3, max torque 239.0

|  |  | Dyno plot: Added Buschur Racing turbo-back exhaust Max hp 240.5, max torque 256.4

|  |  | Dyno plot; Added S-AFC Maximum hp 271.6, maximum torque 253.3. Note dip in torque at 4500 caused by factory boost control solenoid.

|  |  | Dyno plot: Added boost controller 6/11/03 We ran the boost at about 19 psi, tapering to 18 or so at redline. Max hp 275.6, max torque 251.4.

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